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胡状联合站、集输站和计量总站负责胡庆油田油气水的处理,由于设计处理能力严重过剩,开式流程油气损耗严重,工艺管网不合理,设备老化,高耗低效,制约了生产的正常运行。通过一年的技术改造,三座处理站已经投入密闭运行,通过各项生产数据的分析,证明此次改造达到了优化流程,加快集输速度,降低能耗,减少油气损耗,回收富余天然气,提高系统效率的目的。
Hu Lian joint station, gathering stations and measurement terminus is responsible for the oil and gas water treatment Huqing Oilfield, due to serious design and processing capacity surplus, open process serious depletion of oil and gas, process pipe network unreasonable, aging equipment, high efficiency and low efficiency, restricted Production of normal operation. Through one-year technical transformation, the three treatment stations have been put into operation in airtight manner. Through the analysis of the production data, it is proved that the transformation has reached the optimization process, speeding up the gathering and transportation, reducing energy consumption, reducing oil and gas losses, recovering surplus natural gas, Improve system efficiency.